Currently in the flat twin hub, ill get onto that later. I saw this Jowett a about 2 years ago at a club gathering, not knowing a year later I'd make an offer on it and it would be added to the fleet! Just like all unexpected parenting another one to the fleet list three is manageable!
So anyways 1935 Jowett Weasel Sports Tourer, the Jowett flat twin engine which should have had a twin carb setup, but over the years with its problems has been removed and sadly all crucial parts lost in its life time. This is one of the four known of the 75 built over the short run of two years. Aluminium bodied, four seater tourer.
This one has had alot of stick over its life time, lots irregularities and wrong bits including the front wings when I got it. So my basic plan is to get it as correct as I can, fix everything that needs fixing, making it safe and eventually when funds allow it would be nice to get it looking nicer. Since I got it I've sourced the correct wings, re made the correct hood frame, cleaned up the dash, I'm in the process of re-wiring, as the birds nest was looking to light up like Christmas behind the dash a spaghetti of spliced and chocolate blocked wires! And yes that is a massive hole in the radiator, which surprisingly being blocked off still held water!
A few more photos of the rear end, I've replaced the horrible non original lights and after market wing lights. Welded up the holes in the wings, and gave them a slight spray of paint. Painting is not my forte, but they have come out pretty well. Along with a photo of the dashboard cluster which I'm currently sorting out.
Post by 07lilredwagon on Nov 16, 2020 13:51:13 GMT
It amazes me what was done with such a small powerplant!...Though the car is not big by any stretch, that little motor probably did just fine. What a great and rare find/save. I think we might know someone else who knows a bit about Jowetts too, eh?
What is a "Numax" with the warnings on it, Im guessing a power pack of some sort? wild guess, of course.....
Alloy Crank case, and inlet manifold, cast barrels, crank, rods. Yeah that is the rather crude choke, just pull back the elephant ears and it is on choke. To remove the engine you have to undo the steering column and pull it up into the car as its mounted between the barrel and inlet manifold.
Ha the "Numax" is the 12v battery, and that is the battery compartment, in between the two tool boxes either side!
The "sport bit" would have been the twin carbs, no other model sported twins, double valve springs, "uprated" cam shaft & back axle but no idea on the technicals. Though if it survived I wouldn't know until actually taking it apart, maybe one day! I'm looking forward to getting on with it having been busy with work stuff and house stuff throughout this lockdown.
A few more evenings spent on the wicked weasel! Having stripped down the dash before the first lockdown, cleaning up the gauges and replacing some of horrible cracked rusty ones, filling in holes that shouldn't be there and giving it a fresh coat of gloss. I have finally finished most of the wiring now and got everything working. The petrol gauge was a bit of a pain, worked well on the bench, but had a bit of wiring tracing and earthing problem once in the car. All over the hill and pretty pleased with the results. Its now tidy and functional, rather than immaculate just yet. I've still got the surrounding dash to spruce up and sort out. But progress is progress!
Although the MGs T series has clocks in their speedos! Though the TA was 36, this is 35 ahead of the curve for clock placement or just following a trend... It was also passenger side mounted!
A bit more progress on the Weasel, a few more wires added for the dash/map lights. I've wired them in for now as I'm undecided whether to keep them or not. Ideally they shouldn't be there, but removal is a fair bit of work on the dash at present, fixing and repairing the horrible holes that they leave behind. A few photos of the rear number plate with the correct lights painted and working. Plus what the old wiring loom looked like under the dash!
Ha! Your right it doesn't! No idea why its such a spag bol of wires, even had some of those devil made blue splicing clips! I am wondering what went through the guys mind!
Small progress on the little weasel that will one day venture out on the road! Sourcing a pair of "Budgie" Mirror. Mirrors which show whether the trafficator has popped out. Having found one in reasonable condition on ebay, I was gifted one by a facebook group member to repair. So after again finding a small mirror the right size to replace to old knackered one it hasn't turned out too bad. I've also been trying to find a missing piece of the folding windscreen mechanism which happened to be made for luckily not just a Jowett! (Also found on MG J types!)
A month has flown by. Here are a few photos of Weasel tinkerings. Fitting the budgie mirrors properly. Cleaning the gunk from the inlet manifold. Having spent last week off work, I thought it was the perfect opportunity to have ago a making a pattern for the hood lining, I've put together a few mg one in the past, but never had ago a making one from scratch. So a batch order of pattern material then being let loose with a marker pen and scissors here are a few photos of the current hash out. Yes there are lots of ovals on that cardboard... It looked easier on Youtube!
Very much so! The proper double duck hooding is about £50.00 a metre so really REALLY don't want to muck it up! I spent the winter before last remaking the hood frame which took months! Luckily there is another weasel hibernating down in deepest darkest clotted cream country. The Jcc are are good bunch always happy to chat and help out when they can on the subject of Jowetts. So a few photos have been exchanged as to what it should look like. Its the edges I'm worried about!
In the mean time the radiator has been re cored. No more horrible hole and should be nice and cool for Revival taxi duties if we are ever let out again. Next on the list is to sort out the shell and repair/move the starting handle hole lower to the proper place without fouling on the handle.
So things have moved on a bit! Radiator fitted! Radiator shell fitted though I'm convinced now it is the wrong shell. Trying to find another would be like hens teeth I would imagine, so I've made the best of what I have for now. With all of the above fitted, the last bit of wiring done. I've managed to get it out for a short run today, though it seems to be struggling a bit, I think it may need a good flushing out of old fuel and cleaning of the pump. But never mind that, here is a photo finally away from the garage enjoying a brief run out in the sunshine!